|
|
|
|
Day One:
On day one, Saturday, we were
only in the shop for a few hours. I had
driven all night, so motivation was a little low. The only thing we did
was look for a mounting location for the Turbo, see how the exhaust
would route to it and how the down pipe would
route from it.
The location of the turbo was
also dictated by the desire for a noninvasive design. Only the power steering line
needed to be moved. Nothing else needed to be relocated.

The down pipe comes out between the K member and the engine mount, but
sits low enough to allow the use of a full sized filter. I'm probably
still going to switch to a low profile design and will post the part
number once I find it.
Here
is the power steering line. I missed
getting a picture of the stock orientation,
but it comes down and then routes over towards the passenger side and
then back again. This is Ford's idea of a cooling system. I
unbolted the mounting bracket from the K member, With a
wrench on the sensor, the line was carefully bent out of the way
to
clear the way for the 2.5 inch piping that would bring exhaust gases to
the turbo.
I
also started looking at how the IC piping would have to be routed. NO cutting and
as little bending as possible was the rule of thumb. As
a result 2.5
inch intake
piping was used from the turbo to inside the engine bay, where
it transitions to 3 inches just before the MAF sensor. The 2.5 inch
pipe will not result in a restriction on a
sub 500 HP application.

Looking up from under the car into the drivers side of then engine bay.
The pipe comes into the bay right by the stock air box.
Sunday: The
Real Day One
Exhaust to turbo:
Just a note. I helped figure out some routing issues. I helped hold
things in place and had some input here and there on routing. Sometimes my input
was considered, sometimes it was not... I know how to weld with a MIG,
but have never used a TIG and thus did no welding during the
fabrication of this turbo system. I know my way around cars as good as
any back yard mechanic and have pretty good knowledge of turbo systems. However,
I am not a fabricator. I did very little during the assembly of the
exhaust portion or intake portion of the build. I just made it work
once it was all put together via vacuum line installation, MAF
pigtail relocation, gauge installation (again no cutting required, not
even into the firewall) and the eventual tune via an Xcalibrator 2 and
Advantage Software.
Another thing to note: This is not an automotive machine shop. The
owner does custom exhaust and headers, and even builds custom race
cars on the side, but the shop is primarily set up for
aluminum construction components, big machine steel and
aluminum components like press rollers, and aluminum railings.
Below you'll find all the images on the front side of the exhaust. We
worked from the turbo back to where the pipes coming from the CA Ts
would form the Y and joined them together with a flex pipe.
Day Two and
Three:
I did not get a chance to transfer the pictures from
the camera at the end of day two so things are a little mixed. The day started off with the completion of the exhaust from the CATs to
the turbo and fabrication of the downpipe flange, downpipe, wastegate
plumbing and wideband O2 bung. I'm not fond of the placement, but the
reading is only about 0.2 out.

The intercooler in the background is mounted. There was one sitting
around that used to be on a 500 HP DSM and it fit right up under the
cover. This was actually done up on day 1 when I
wasn't looking. It measures 29 inches from tank to tank, 10 inches high
and is three inches thick
The power steering pressure line is the only
stock part on the car that needed relocating. There is more
than enough clearance between the hot pipe that runs to the
turbo and the power
steering line. The line is also still in the direct path of
air going under the
car for cooling. To date, I've had no problems with heat where the
power steering is concerned, even at idle and in stop and go traffic.
The oil drain line: This is the most invasive part of the
install.
The 4.0 has a
remarkable bottom end design. The mains are actually
integral to the oil pan, so instead of pulling off the entire pan,
there is a nice little access panel. Great idea right? Well, if you
don't subtract points for execution, then yes. The panel is better then
having to remove the entire engine to get the pan off, but it's
placement makes getting to some of the bolts a little difficult. A
small bend in a box end wrench will make this task much easier.
We began day five
by lowering the car for the first time
since I arrived... for more than 2-3 minutes at least. While the turbo
intake pipe was being made, I pulled off the airbox and set it
aside, cut
the stock valve cover evac hose off and routed a length of 5/8s oil
resistant hose from the turbo inlet to the valve cover.
Work continued on the intake piping for the IC to turbo connection
on the drivers side. This was the more complicated of the pipework
coming into the engine bay. Due to space it was the only area we made a
slight bend in the core support so the IC to bay pipe could be slipped
in and removed with ease.
With the blowoff
valve
installed into the
turbo to IC pipe, it was time to set up the vacuum lines. For now, I
only needed
three connections; one for the wastegate, one for the blowoff and one
for the boost gauge. Installing the boost controller was going to be
quite involved due to it being in-car, so I left that project for
another day.
The
pictures above
and to the left show the line
coming from the primary T to the firewall and then going down towards
the transmission tunnel. It wraps tight along the underside of the
tranny into the wastegate actuator.
Day 6 is not documented with many images. After running around trying
to figure out if there was anything we could do to the GT drive shaft
that showed up about noon, I focused on swapping the 7.5 back into the
car. While the exhaust was being tied up, I routed the boost and wideband lines
into the interior, slipping them in through the passenger side fender
into the door jam and then into the car.
It was 6:30PM on day 6 when we started the car for the first time since
I got there. It fired right up. No hesitation, no learning, no cell and
no limp... she just purred like a kitten. We lifted the car up one more
time to check for exhaust leaks and to our surprise and pleasure there were none at all.
The boost gauge was hooked up for
the trip back home, but the wide band
still needed power. I was in a hurry and at about 9 PM decided just to hack a
phone charger
and use the lighter plug to get it going before I left IL... about 5
hours after I got the gauge in, I was on the road for 900 miles! No
further testing, just a 91 Octane SCT Strategy Flash cookie cutter
tune. I could hear the turbo every time I left from a stop and
occasionally at the top of second and third... Those of you who have
owned turbo cars can just imagine the amount of discipline it takes to
NOT push the throttle to the floor. Try it for 14 hours straight. Hah.
I got caught playing with a GT in PA up a long hill - 81 I think - and
pulled a lean condition bank 2 cell. oops.
|
|
|
|
|